Add option to move away from endstop after homing.
- Add `ENDSTOP_BACKOFF` for printers with a recessed Z home button (Lulzbot TAZ 6).
- Also prevents chattering when sensorless homing with axes against bumpers.
Allow `ENABLED`, `DISABLED`, `PIN_EXISTS`, and `BUTTON_EXISTS` to take multiple arguments. Also add:
- Alias `ANY(...)` for `!DISABLED(...)`
- Alias `ANY_PIN(...)` for `PIN_EXISTS(a) || PIN_EXISTS(b) ...`
- Alias `EITHER(A,B)` for `ANY(...)`
- Alias `ALL(...)` and `BOTH(A,B)` for `ENABLED(...)`
- `NONE(...)` for `DISABLED(...)`
* Multi-nozzle selective duplication
* Use a bit-mask, reduce stepper_indirection.h size
* Tweak the multi-nozzle duplication description
* Use 'S' as a bool in M605
* Add HAS_DUPLICATION_MODE conditional
* Remove '_MODE' from the option name
* M605 in the style of Stacker M280
* Also include direct mask style (P)
- The `sdcard.transfer_port` variable is Marlin's internal serial port index, not the physical serial port number.
- Added packet number to "ok" response so hosts don't need to wait for the ACK.
- Renamed feature to `BINARY_FILE_TRANSFER`, as the speed up is only consequential to the ability to transfer binaries over serial.
* Add Formbot Raptor board
Co-Authored-By: InsanityAutomation <insanityautomation@users.noreply.github.com>
* Add a second Z probe Z offset
Co-Authored-By: InsanityAutomation <insanityautomation@users.noreply.github.com>
* Modify method to utilize live adjustment of hotend z offset
Should probably move config option to babystepping and rename as it may now apply to all multiextruder systems
* Move config item and catchup other code to current method
- Respect axis max acceleration limits instead of forcing a fixed acceleration value.
- The `junction_unit_vec` ensures proper handling of entry and exit speeds even when the axes involved have different limits.
This is an initial cut for feedback, updated for 2.0.x.
Chamber temperature is currently reported along with hot end and bed
temperatures to serial. The format is just like that used for hot end
and bed temperatures, but using 'C' prefix. As there is no heater,
target is always 0. Is this appropriate, is there a better way to report
chamber temperatures?
Chamber temperatures are not reported on the LCD in any way.
When auto chamber fan is enabled, it currently just uses the same
temperature threshold as the other auto controlled fans.
As the chamber temperature is not connected to any heater, it doesn't
undergo mintemp/maxtemp monitoring. This would need to change in the
future if chamber heating became a feature.
Some users may prefer to hide the position updates on the `LIGHTWEIGHT_UI` altogether. This leads to an even less cluttered display (it also saves on SPI traffic and one byte of RAM).
- This status screen uses the ST7920 character generator to greatly
reduce SPI traffic and MCU load when updating the status screen.
- Has been tested with the RepRapDiscount Full Graphics Smart Controller
but should work with any LCD that uses an ST7920 or fully compatible
controller.
Updating I2C position encoders to enable babystepping and Babystep XY when using the ecm microstep correction method. Also changed default method to ECM microstep.
- Fix G26 Circle Drawing.
- Add default extrusion settings so machine can print lines on print bed
- Yet to be done: Get LCD Menu's to use these settings.
* Re-Print of same SD Memory Card file with single click
* Re-Print of same SD Memory Card file with single click
* This is the bugfix-v2.0.0 version of https://github.com/MarlinFirmware/Marlin/pull/8104
* Add MAX7219_DEBUG to Travis CI testing
* Tweak config and use standard pin naming for MAX7219_DEBUG
* MAX7219: Apply coding standards, use macros, etc.
* Make code work...
* [New Feature] I2C position encoder support
I plan to continue improving/cleaning this up, as there areas that need work.
* let the cleanups begin.
* progress
* more progress
* comments, rename files, etc.
* clean
* Cleanups per thinkyhead
* a few more cleanups
* cleanups, bugfixes, etc.
* remove unnecessary passes_test(), additional cleanups/optimizations
* cleanups
* misc.
* Fix up I2CPEM.init() and a few other things.
* organize, fix, rename, etc.
* more optimization
* a few more tweaks
==============================
Configuration_adv.h changes
==============================
add "live" LCD update
==============================
P & S version
==============================
final (hopefully) tested version
==============================
update M115 capabilities print
==============================
Menu changes portion of the requested changes
==============================
changed USEABLE_HARDWARE_PWM from a function to a series of macros
==============================
changes per review
The menu (commands / scripts) is configurable in `Configuration_adv.h`.
- Added conditionals.
- Changed script handling.
- Slimmed and working!
- Added Status message.
- Returning to lcd status screen now!
- Example Configs Updated.
- Cleanups by @thinkyhead
* Unify M600 and M125 pause features
* Cleanup per thinkyhead's comments
* Rename filament_change_menu_response to advanced_pause_menu_response
* Include HAS_BED_PROBE in QUIET_PROBING
* Update gMax example file
* is_idle() is out of scope without the braces
* Convert FT-i3-2020 to Advance Pause names...
* Allow pause even if not printing
- fix broken `M421` due to less-than-careful optimization
- add HOME_AFTER_DEACTIVATE define to advanced config so not everyone has to rehome after steppers are deactivated
- misc. cleanups (remove unused label, unused variables)
add BLTouch-related messages in english and (rusty) french;
add missing endstops.h in ultralcd.cpp;
fix misc. compiler warnings;
fix lsf_reset - ZERO macro can't handle a pointer as it would only memset the size of the pointer, not the size of the entire struct
* relocated ubl state to config. store:
* removed a number of ubl state variables and padding which were largely unused - saved 58 bytes of both SRAM and EEPROM;
* modified ubl sanity_check - no longer checks removed state variables that were otherwise unused, where checking didn't seem to accomplish anything, ultimately;
* removed pre_initialized state, saving 64 bytes of SRAM;
* removed automatic saving of UBL state after UBL activation/deactivation;
* consolidated multiple GRID_MAX_POINTS_X/Y to 'Global Leveling' section of EEPROM;
* minor update to G29 Sx notes/instructions;
* renamed mesh load and save parameter to 'slot' from 'm' for clarity;
# This is the 1st commit message:
MCP4728 consistency & fix ultralcd.cpp
The MCP4728 DAC controls the stepper motor current strenth on the
PRINTRBOARD Rev F and RIGIDBOARD V2 boards.
PR #5792 on 9 FEB 2017 implemented default drive percentages but only on
the RIGIDBOARD V2.
This change moves the default settings to Configuration_adv.h.
Also, ultralcd.cpp won't compile because of a type def conflict.
Changed it to match the one in stepper_dac.cpp
===========================================================
reword stepper curent section for clarity
===========================================================
change name & improve comments
===========================================================
changed name from A4JP to SCOOVO_X9H per PR #6139
# This is the commit message #2:
fix typo
The offset for Z_DUAL_ENDSTOP (z_endstop_adj) is already in Marlin.
This PR just makes it a configuration item.
z_endstop_adj is initialized in two places so both had to be modified.
Made the double touch portion a conditional compile based on the
PROBE_DOUBLE_TOUCH flag.
==============================================
Bugfix
The current G38 only stopped a move if it involved the Z axis.
Moved all the G38 code to it's own section and put it where it would
always be executed no matter what axis was moving or if the endstop was
enabled.
Also added a comment to configuration_adv to alert the user the double
tap had to be turned on.
==============================================
Change G38 back to using Z_MIN_PROBE
There's no Z_MIN endstop if Z_DUAL_ENDSTOPS is enabled and you have them
set to the top of the gantry.
G38 started out as using the Z_MIN_PROBE pin. I don't remember why we
changed it to the Z_MIN endstop.
The target here is to update the screens of graphical and char base
displays as fast as possible, without draining the planner buffer too much.
For that measure the time it takes to draw and transfer one
(partial) screen to the display. Build a max. value from that.
Because ther can be large differences, depending on how much the display
updates are interrupted, the max value is decreased by one ms/s. This way
it can shrink again.
On the other side we keep track on how much time it takes to empty the
planner buffer.
Now we draw the next (partial) display update only then, when we do not
drain the planner buffer to much. We draw only when the time in the
buffer is two times larger than a update takes, or the buffer is empty anyway.
When we have begun to draw a screen we do not wait until the next 100ms
time slot comes. We draw the next partial screen as fast as possible, but
give the system a chance to refill the buffers a bit.
When we see, during drawing a screen, the screen contend has changed,
we stop the current draw and begin to draw the new content from the top.
lcd_update can take so much time that the block buffer gets drained if
there are only short segments. This leads to jerky printer movements for
example in circles and a bad print quality.
This change implements a simple check: Only if the block currently
executed is long enough, run lcd_update.
This also means the printer will not show actual values on the LCD nor
will it respond to buttons pressed. A option that keeps the menu
accessible is also available.
Aditionaly, slow down if a block would be so fast that adding a new
block to the buffer would take more time. In this case, the buffer would
drain until it's empty in worst case.
1) modified 3 code files
Marlin.h
Marlin_main.cpp
endstops.cpp
2) modified config files so I could test on my machine
Testing was done on an AzteegX3pro based machine.
The probe was hooked to the Z_MIN endstop.
My controller doesn't have a dedicated Z_PROBE input so I couldn't test
that functionality.
Verified that a large file (without any G38 commands) executed the same
before and after the changes.
Verified that the head moves as expected when G38.2 and G38.3 commands
are issued. Single & multiple axis moves were tested along with + and -
directions.
Code was added to the main ISR. In normal operation only one extra IF
statement is evaluated. I didn't notice any performance degradation
because of the added code.
The G38 commands are expected to be issued manually by the operator
during machine setup. The G38 commands wait until the machine is idle
before proceeding. That way the other commands are minimally impacted
by the extra ISR overhead when a G38 command is in the queue.
The G38 commands are very similar to the G28 commands except 1) only the
Z_PROBE is used and movement can be in the + or - direction.
See issue 4677 for a discussion on adding G38 commands to Marlin.
Feature request: add ability to use G38.2 command (CNC)
MarlinFirmware/Marlin#4677
About Configuration.h:
・Fix the PR #4899 (ABL: Enable by type. Bilinear for all.)
Remove Duplicated contents
・Fix the PR #4305 (Custom boot screen feature improvement)
Revert from "during boot" to "during bootup" in all the example
Configuration.h
・Fix the PR #4207 (Clean up, simplify and generalize the Allen-key-probe
code.)
Resolve and relocate the duplicated definitions in Z_PROBE_ALLEN_KEY
section
・Follow-up the PR #4805 (Additional documentation of Configuration.h)
Add forgotten changes to all the example Configuration.h
Adjust spacing
About Configuration_adv.h:
Add missing description of SLOWDOWN for DELTA
Adjust spacing
Similar to the current Arduino HardwareSerial
but with max. 256 byte buffer-size.
Deactivated by default.
The boards with AT90USB processor (USBCON) already use a TX-buffer.
Add an emergency-command parser to MarlinSerial's RX interrupt.
The parser tries to find and execute M108,M112,M410 before the commands disappear in the RX-buffer.
To avoid false positives for M117, comments and commands followed by filenames (M23, M28, M30, M32, M33) are filtered.
This enables Marlin to receive and react on the Emergency command at all times - regardless of whether the buffers are full or not. It remains to convince hosts to send the commands. To inform the hosts about the new feature a new entry in the M115-report was made. "`EMERGENCY_CODES:M112,M108,M410;`".
The parser is fast. It only ever needs two switch decisions and one assignment of the new state for every character.
One problem remains. If the host has sent an incomplete line before sending an emergency command the emergency command could be omitted when the parser is in `state_IGNORE`.
In that case the host should send "\ncommand\n"
Also introduces M108 to break the waiting for the heaters in M109, M190 and M303.
Rename `cancel_heatup` to `wait_for_heatup` to better see the purpose.
Includes:
*firmware version / branch / date.
*extruder count
*board information (name, serial details, power supply type)
*thermistors (names, min/max temperatures)
*printer statistics (PRINTCOUNTER details)
Thanks to @thinkyhead for contributions.
No compromises for the manage_heater(). manage_heater() will return immediately when there is nothing to do, but needs a constant detaT to work proper.
Calling idle() only every 200ms results in a display update every ~2 seconds - that should be enough.
For the other functionalities in idle() and manage_inactivity() 200ms is a lot but hopefully works.
When setting the bed temp via M140/M190 if the thermistor does not read an increase of WATCH_BED_TEMP_INCREASE degrees by WATCH_BED_TEMP_PERIOD seconds then it will throw "Error:Heating failed, system stopped! Heater_ID: bed" and call the kill() function.
Conflicts:
Marlin/Configuration_adv.h
Make stepper shutdown after inactivity dependent on a new set of
#defines.
DISABLE_INACTIV_X
DISABLE_INACTIV_Y
DISABLE_INACTIV_Z
DISABLE_INACTIV_E
And make exemplaric Configuration.
Names can be discussed.
This makes the disabling of the steppers independent from the DISABLE_?
settings witch shut down the steppers immediately.
- `SD_DETECT_PIN` replaces `SDCARDDETECT`
- `SD_DETECT_INVERTED` replaces `SDCARDDETECTINVERTED`
- Revise the description of `SD_DETECT_INVERTED`
- Add a note about the override of `SD_DETECT_INVERTED` in
`Conditionals.h`
As suggested in #2521
- Move `ABORT_ON_ENDSTOP_HIT_FEATURE_ENABLED` because `SDSUPPORT` is
also required.
- Add a note that endstops must be enabled for the feature to have any
effect
- Make thermal protection for all hotends and/or bed into simple
switches
- Now enable `WATCH_TEMP_PERIOD` when `THERMAL_PROTECTION_HOTENDS` is
enabled
- Move detailed thermal parameters to `Configuration_adv.h`
- Add sanity checks to warn about old configurations
- Change `WATCH_TEMP_PERIOD` to seconds instead of milliseconds
- Add “Level Bed” menu item for auto bed leveling
- Hide the option if homing has not been done yet
- Arrange the Prepare submenu more logically (?)
- Add documentation comments, some white-space
- Apply some coding standards here and there
- Move old encoder multiplier debug option to `ultralcd.cpp`
This addresses comments in #1956 and #1079. In particular, this is useful
when both endstops are stationary on a CoreXY system, and the Y axis needs
to be homed before the X so the flags are aligned.
With these changes the output of `M503 S0` is all you need to restore
the EEPROM. Building on this it is straightforward to save and restore
the EEPROM state using the SD card or external GCode file.
- Added `M145` to set “heatup states” for the LCD menu
- Added `M420` to toggle Mesh Bed Leveling
- Added `M421` to set a single Mesh coordinate
- Extended `Config_PrintSettings` with added M codes
- Cleaned up some comments here and there
Z_DUAL_ENDSTOPS is a feature to enable the use of 2 endstops for both Z
steppers - Let's call them Z stepper and Z2 stepper.
That way the machine is capable to align the bed during home, since both
Z steppers are homed.
There is also an implementation of M666 (software endstops adjustment)
to this feature.
After Z homing, this adjustment is applied to just one of the steppers
in order to align the bed.
One just need to home the Z axis and measure the distance difference
between both Z axis and apply the math: Z adjust = Z - Z2.
If the Z stepper axis is closer to the bed, the measure Z > Z2 (yes, it
is.. think about it) and the Z adjust would be positive.
Play a little bit with small adjustments (0.5mm) and check the
behaviour.
The M119 (endstops report) will start reporting the Z2 Endstop as well.
- Add `Conditionals.h` with calculated configuration values
- Add `SanityCheck.h` with checks for configuration errors
- Remove equivalent code from all configurations
- Move error checks from some sources to `SanityCheck.h` also
- Fix initialization of count_direction in stepper.cpp
Small changes (and formatting to confuse the diff’er) which first
allows DOGLCD and LCD_PROGRESS_BAR to be enabled in tandem, then a
#warning (rather than error) that the extra progress bar / message
options don’t apply to graphical displays at this time. This leaves
open perhaps combining the progress bar and message area in some future
(or forked custom) graphical LCD display arrangement (at which time the
relevant variables may be moved into ultralcd.cpp with externs in
ultralcd.h). I also added a conditional error that the progress bar and
the filament display may not work well together.
- Fixed issue when BAL area probing is shorter than it should be for
grid probing
- Warning when BAL activated with Delta Kinematics
- Fix XY_TRAVEL_SPEED when homing Z axis
Tosh stepper drivers need to be driven slower, so the stepper code
was interleaved to separate the pin HIGH from the pin LOW. This adds
enough instructions to make it work, without needing nops.
FW retraction is extended onto swap retraction invoked by 'G10 S1'.
Bookkeeping of the retract state of all extruders allows for having one
extruder fw standard retracted while another extruder is swap retracted.
An LCD menu item for the swap retract and recover length was added.
Firmware retraction now stores the retract and recover speeds in mm/s
instead of mm/min. This makes it match the units of the maximum
feedrate, and fixes problems with modifying the value via LCD control
panel. From gcode, the values are still taken in mm/min to match the
units of G1 and similar, and they are converted to mm/s before they are
stored.
I also lowered the default retract feedrate to make it less likely to
cause problems for geared extruders when the user hasn’t bothered to
set a reasonable maximum feedrate, though users should be setting both
of these values to suit their hardware.
Add digipot i2c control for MCP4451
Allow M907 to set i2c digipot currents in amps
Fix Makefile to allow Azteeg motherboards
Fix Makefile to allow Wire libraries only
Add beeper pin for Azteeg X3 Pro
if you try to enable Z_DUAL_STEPPER_DRIVERS the error "You cannot have dual drivers for both Y and Z" shows even if you don't have defined Y_DUAL_STEPPER_DRIVERS and don't let you compile the firmware
to solve this problem i change this line:
#ifdef Z_DUAL_STEPPER_DRIVERS && Y_DUAL_STEPPER_DRIVERS
to:
#if defined (Z_DUAL_STEPPER_DRIVERS) && defined (Y_DUAL_STEPPER_DRIVERS)
now the error only show if you define both Z_DUAL_STEPPER_DRIVERS and Y_DUAL_STEPPER_DRIVERS
If "SHOW_TEMP_ADC_VALUES" is defined in Configuration_adv.h, the M105
command will present, after tradicional temperatures, the ADC value read
from temp sensors. This is great for adjusting thermistor tables with
thermocouple.
From Pronterface you can see the ADC value and compare with a
thermocouple reading.. then you just need to create your own thermistor
table.
Since this merge doesnt change the original information, it doesnt mess
with PC software parsing (tested under Pronterface and Repetier-Host).
This is _not_ automatically the cronological, since deleting a file will free
the filesystem descriptor for it, which then will be used by the next file copied on it.
Since this makes the auto0.g file very inaccessible, I put the option back, to have it in the prepare menu.
this should satisfy https://github.com/ErikZalm/Marlin/pull/373
as a reminder, auto0.g will be executed every time after a boot with sd card present and file present.
thereafter, if there is a file auto1.g this will be done. Thats IMHO the best place to put settings, and prepare heating.
I also execute again after each (now again via the prepare menu) before starting a new print/ after a failed one.
It for me 100% replaces any start.gcode form the slicers.
also, removed some trouble for compilation with corexy.
I think that babystepping is only possible in z for a delta tower.
not sure if it would be usefull to step individual motors on a delta, i don't own one
It is a realtime control over the head position via the LCD menu system that works _while_ printing.
Using it, one can e.g. tune the z-position in realtime, while printing the first layer.
Also, lost steps can be manually added/removed, but thats not the prime feature.
Stuff is placed into the Tune->Babystep *
It is not possible to have realtime control via gcode sending due to the buffering, so I did not include a gcode yet. However, it could be added, but it movements will not be realtime then.
Historically, a very similar thing was implemented for the "Kaamermaker" project, while Joris was babysitting his offspring, hence the name.
say goodby to fuddling around with the z-axis.
Enables two stepper drivers to be used for the Y axis (useful for
Shapeoko style machines)
Each Y driver can be stepped in either the same way or in opposite
directions, accounting for different hardware setups (leadscrew vs. belt
driven)
Enables two stepper drivers to be used for the Y axis (useful for
Shapeoko style machines)
Each Y driver can be stepped either the same way or in opposite
directions, accounting for different hardware setups (leadscrew vs. belt
driven)
[default off for now]
syntax: M600 X[pos] Y[pos] Z[relative lift] E[initial retract] L[later retract distance for removal]
if enabled, after a M600, the printer will retract by E, lift by Z, move to XY, retract even more filament.
Oh, and it will display "remove filament" and beep like crazy.
You are then supposed to insert a new filament (other color, e.g.) and click the display to continue.
After having the nozzle cleaned manually, aided by the disabled e-steppers.
After clicking, the printer will then go back the whole shebang, and continue printing with a fancy new color.
Add a feature to run the cooling fan at full speed for a small period
(default 100ms) when first starting the fan. Some fans wont reliably
start spinning at low power, and many fans have issue with the PWM at
low power. However, once the fan starts spinning it can reliably be
set to a wide range of PWM values.
fixes#246
Added statements to set the limit switch positions to the maximum travel if homing in the positive direction as well as bed center at (0,0) if defined.
Relocated code based on feedback.